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Title: METHANE DE-NOX FOR UTILITY PC BOILERS

Technical Report ·
DOI:https://doi.org/10.2172/823152· OSTI ID:823152

During the current quarter, pilot-scale testing with the modified air nozzle version of the PC burner was completed with PRB coal at the Riley Power Inc. (RPI) test facility. A total of 8 different burner configurations were tested utilizing various burner air nozzle arrangements in place of the burner air channels. It was found that with the arrangements tested, a stable flame could not be maintained at coal feed rates above 100 lb/h. While it is felt that the air nozzle approach can ultimately be used effectively, in the interest of holding to the current project schedule it was decided to proceed with the balance of the project using the air channel design. The pilot-scale PC burner was therefore restored to the air-channel configuration and benchmark testing with PRB coal to confirmed previous operating results. A series of tests was then conducted with PRB and West Virginia caking coal to evaluate modifications to the gas combustor configuration and operation for improved performance with caking coal. Continuous operation was achieved with caking coal up to 50 lb/h vs. the full load target of 150 lb/h. Impingement and deposition of partially devolatilized coal occurred at various points within the combustor when the caking coal feed was increased above 50 lb/h. The 100 MMBtu/h commercial-scale prototype design was started with coal burner design input from both RPI and VTI. Based on typical burner installation layout considerations, it was that the preheat combustor should be oriented horizontally on the axial centerline of the coal burner. Accordingly, work was begun to relocate the pilot gas combustor to this orientation so that the pilot results with caking coal will be directly applicable to the preferred 100 MMBtu design. Inspection and repair of the 100 MMBtu/h Coal Burner Test Facility (CBTF) was initiated by RPI and as of 6/30, this activity was 70% complete.

Research Organization:
Institute of Gas Technology (US)
Sponsoring Organization:
(US)
DOE Contract Number:
FC26-00NT40752
OSTI ID:
823152
Resource Relation:
Other Information: PBD: 30 Jul 2003
Country of Publication:
United States
Language:
English