Introduction

The He–Ne laser is commonly used in laboratories as a simple and convenient light source in various experiments and measurements. The coherence time of the laser is very important for many laser applications such as interferometry, speed measurements, laser gyroscopes, and so on. Among these applications, recently the generation of vector doughnut beams and purely single transverse mode vortex beams [1, 2] are also under consideration, for which the periodical change of the intensity and polarization distributions of the He–Ne lasers can significantly affect the final outcomes. Therefore, the thermally stabilized He–Ne lasers play a very important role to improve the experiments’ results.

In recent years, many scientists, owing to a high ability of He–Ne lasers for stabilizing in the Doppler line width range, have focused their attention on the enhancement of coherence time. In 1972, Balhorn et al. established the frequency stabilization theory in this type of lasers for the first time [3]. To stabilize the frequency of laser light, they controlled the voltage of laser power supply by using intensity changes arising from temperature variations. Their effort leaded to the stability of Δν/ν = 1 × 10−7 (30×). In addition, after 1973, Bannet et al. achieved the stability of 2 × 10−8 (160×) by the heating coil method [4]. Since then, passive and active methods with different designs and techniques have been developed for frequency and amplitude stabilization of He–Ne lasers, which has resulted in the stability of ∼10−16 (~1010×) [518].

As seen in previous researches, in the first approximation, the stabilization is normally carried out by controlling the length of the laser. In the case of internal-mirror He–Ne lasers, the length of the laser can be controlled by adjusting the temperature of the laser tube. For this purpose, generally, the current of a strip heater wound around the laser tube can be controlled by an electronic circuit. Although in this method one can achieve a quite high stability, ∼10−9 [19], using a heater may change the original features of laser tube, making the stabilization process more difficult due to additional temperature increase in the laser tube, which in turn reduces its lifetime. To overcome the problem, in 1982 Sasaki et al. [14] controlled the temperature of the laser tube by a cooling fan and obtained a stability of ∼10−8 by this procedure. In 2012, Qian et al. achieved a stability of 4.3 × 10−9 by removing some drawbacks. They realized that the short-term stability may be limited by mechanical vibration of the fan and air flow, which can be improved by utilizing a mini cooling fan with lower vibration. In addition, to achieve a smoother rotation of the fan, they optimized the drive circuit [15]. Although the use of fan apparently prevents the temperature rise of the laser tube, the least disruption in the fan revolution adjustment severely affects short-term stability. To control the length of laser cavity, Ellis et al. utilized a Peltier thermoelectric cooler in 2010 and 2012 [16, 17]. They used a mixed mode within the optical cavity to stabilize the absolute laser frequency. But in the papers, the effect of laser plasma ambient temperature on the output power has not been examined.

In this paper, frequency stabilization of an internal-mirror He–Ne laser is performed by the control of the laser tube’s temperature using two thermoelectric coolers. First of all, the discharge current of the laser is adjusted at the operating point, and then, to prevent the effect of external factors, the laser is isolated from the environment via two thermal and acoustic insulator shells. The laser ambient temperature is controlled via an appropriate electronic circuit using two Peltier thermoelectric coolers around the temperature 23 °C, so that the laser frequency can be stabilized. The advantage of this approach, in addition to adjusting the laser ambient temperature to maximize the laser light power, is to overcome the effect of ambient temperature variations on the laser performance. On the other hand, it should be noted that this method, in comparison to much other techniques, can be more cost-effective.

Experimental

In this study, an internal-mirror He–Ne laser (Model 2500, from supplier: Changsha Aube Didactic Equipment Co., Ltd.) oscillating at the wavelength 632.8 nm, with the maximum power 2.43 mW at the temperature 23 °C, the cavity length L = 24.5 cm, an axial mode spacing of about \(c/2L = 612 {\text{MHz}}\), and without any Brewster windows, was used. The laser does not have any transverse modes. Initially, the number of laser longitudinal modes was measured by a scanning Fabry–Perot interferometer (SF–PI) (Fig. 1).

Fig. 1
figure 1

A schematic setup for measuring laser modes by a scanning Fabry–Perot interferometer (SF–PI): PZD piezoelectric device, M mirror of the SF–PI connected to PZD, P.T photodetector, AMP amplifier

The longitudinal modes of laser were separated by changing the length of SF–PI by a piezoelectric device (PZD) connected to the mirror M. The sawtooth wave generator drives PZD, which controls the vibration of mirror M. The laser light after transmitting through SF–PI is detected by the optical detector (PT), whose electronic signal after amplifying by the amplifier (AMP) is observed via the oscilloscope. The measurement shows that the laser has two longitudinal modes very often, but with the change of laser length arising from the thermal expansion; when one of modes is closed to the central frequency in the gain profile, the third mode may also appear.

Determination of laser principal axes

In gas lasers, owing to the induced anisotropy in the laser mirrors, there exists two orthogonal principal axes for the laser system at a plane perpendicular to the laser light propagation [20, 21]. The refractive indices and absorption coefficients in the direction of these two axes are normally different. On the other hand, calculations show that the polarization of each longitudinal mode in gas lasers is linear and in the direction of one of the principal axes. In addition, the polarizations of successive modes are perpendicular [22]. Here, the direction of laser principal axes was determined using an SF–PI. For this purpose, a polarizer was put in the front of the laser light whose polarization direction is generally arbitrary with respect to the principal axes (x, y). Thus, the laser light after passing the polarizer consists of all longitudinal modes, except that the polarizer transmission axis coincides with each of the two principal axes (x, y), which results in the elimination of one or two of the three modes, as shown in Fig. 2. In this method, the principal axes were determined with an accuracy equal to that of the polarizer calibration (±5°).

Fig. 2
figure 2

Block diagram of laser principal axes measurement by SF–PI: M mirror, P.T photodetector, AMP amplifier

Laser stabilization system

The laser stabilizing system was generally constructed from four parts: the power supply unit, the thermodynamic system, optical components and the stabilizing circuit (Fig. 3).

Fig. 3
figure 3

The block diagram of the stabilization system: HV high-voltage source, ACS adjustable current source, TEC thermoelectric cooler, ABS asymmetrical beam splitter, WP Wollaston prism, PD1 and PD2 photodetectors, DA differential amplifier

The power supply unit Due to the effect of voltage fluctuations of the city electricity and instability of the laser power supply on the ultimate limit of frequency stabilization, an appropriate adjustable current source was designed and fabricated to control the current of the laser discharge tube with the precision ±0.01 mA (Fig. 4). DZ1 and DZ2 consisted of two 5.6 V Zener diodes, operating as a voltage reference with an approximately zero temperature coefficient. By altering the potentiometer P 1 and applying an adequate voltage to the inverting input of the operational amplifier (OA1), the current of the laser tube can be adjusted at an optimal value. Hereafter, any unwanted change in the laser current will be neutralized through the negative feedback loop, including the optocouplers OP1 and OP2, the resistor R 7 and the operational amplifier OA1. The Darlington transistors DT1–DT4, biased through the resistors R 1R 4, provide a voltage ladder as a high-voltage transistor.

Fig. 4
figure 4

The circuit of the power supply unit, including a high-voltage power supply and an adjustable current source

The thermodynamic system: To avoid the effect of thermal and acoustic variations on the frequency stabilization of the laser, in addition to the metallic box of the laser an MDF box whose inner walls have completely been insulated by two thermal and acoustic insulation shells was used. Phenolic with chemical composition C6H5OH and thermal transfer coefficient of 0.018 W/m °C at 24 °C was utilized as the thermal insulator. On the other hand, the material consists of rubber grains of EPDM (ethylenepropylene diene terpolymer), which is made under the hot pressing process in the presence of anti-rupture materials and its acoustic insulation coefficient is 55 dB, was exploited as the acoustic insulator. For keeping constant the temperature of the laser system, two thermoelectric coolers (with 70 W cooling capacity) were connected to the metallic box of the laser through an aluminum block with dimensions (14 × 7.5 × 4) cm. To establish better connection, all surfaces were foremost polished very well. Furthermore, to achieve the best heat energy conduction from the laser metallic box to the aluminum block and finally to the Peltier coolers, the paste of zinc oxide (ZnO2) was utilized as the interface. The reason for the use of ZnO2 is its much larger thermal conductivity (200×) compared to air existing in the microscopic bumps between surfaces. To connect the Peltier thermoelectric coolers to the aluminum block and also the aluminum block to the laser metallic box, eight springs were used. The hot surface of each thermoelectric cooler was connected to an aluminum heat sink with dimensions of (7.6 × 6.7 × 4) cm that is cooled by a high-speed fan (Fig. 5).

Fig. 5
figure 5

The manner of connecting the two thermoelectric coolers on the laser box

Optical components: As seen from Fig. 3, a slight part of the laser light is sampled by the asymmetrical beam splitter (ABS) and steered toward the Wollaston prism (WP). To remove the problems related to the optical feedback and interference effects, ABS was set at an angle of about 10 ° with respect to the output light wave front. By properly adjusting WP, the sampled light beam is split into two separate beams with linearly orthogonal polarizations associated with the principal axes of the laser. The signals related to the intensities of the two beams, detected by the photodetectors PD1 and PD2, are delivered to the stabilizing circuit.

The stabilizing circuit: Figure 6 shows the stabilizing circuit in detail. At first, the switch S is in position A, and the current of thermoelectric coolers, by changing the amplification coefficient (R 4) and the input voltage (R 2) of amplifier OA1, is adjusted so that the laser ambient temperature is fixed at the optimal temperature. The transistors T 1, T 2 and T 3 provide the necessary current for the thermoelectric coolers. R 17 and R 18 are ballast resistors that divide the coolers’ current equally between T 2 and T 3. After fixing the temperature of the laser ambient, by putting the switch S at position B, the control of the thermoelectric coolers is conceded to an integrator whose input is the signal of intensity difference of two principal modes. The amounts of R 10, C 1 and also R 10 C 1 are so determinant in the ultimate frequency stability, and normally they are empirically specified.

Fig. 6
figure 6

The stabilizing system, including the feedback and cooling circuits

Results and discussion

Since in He–Ne lasers, there exists an optimal current of laser tube in which the power of the laser light can be maximized [23], first of all, the laser power versus different discharge currents was measured by a power meter (including the optical sensor XLP12-3S-H2-D0 and the power monitor MAESTRO, from Gentec) at the equilibrium temperature of the laser with its ambient, 46 °C. Then, the best-fitting curve of the experimental points was plotted (Fig. 7). The figure shows that the optimal current of the laser tube corresponding to the maximum power is 5.5 mA.

Fig. 7
figure 7

The laser power versus discharge current: blue dots experimental data; green line the best-fitting curve of the experimental points

Therefore, to find the amount of ballast resistor (R Ballast) in Fig. 4, in addition to the current of the laser tube, the operating point voltage of the laser was also needed to be obtained. For this purpose, the voltage of the laser tube was measured versus different discharge currents using an adjustable current source. Figure 8 indicates the best characteristic curve of voltage versus the current of the laser tube (red line), plotted by the use of measured experimental data (blue dots). The operating point of the laser (Q) can be obtained from intersecting the DC load line of the laser (green line), that is, V laser = 2600 − R B I laser (V), and the characteristic curve by considering I laser = I opt. = 5.5 mA.

Fig. 8
figure 8

The laser voltage versus discharge current, used for determining the operating point of the laser

The inspection indicated that the operating point voltage is equal to 1560 V and, therefore from the DC load line, R B was obtained to be 189.1 kΩ. Since R B involves R Ballast and the equivalent resistor of the high-voltage transistors (Fig. 4), by considering the most stability of discharge performance of the laser, R Ballast was selected equal to 180 kΩ. After adjusting the current of the laser tube to the optimal value, 5.50 mA, it was a question for us if there was a temperature at which the laser output power was maximized.

To answer this, by using thermoelectric coolers, the laser output power in terms of different temperatures from 5 to 50 °C was measured and plotted (Fig. 9). As observed, the optimal temperature, that is, the temperature at which the laser power is the maximum, is about 23 °C. Therefore, it is reasonable that the laser stabilization is carried out at the optimal temperature. The lasing at this temperature leads to two advantages: having maximum laser output power and increasing the laser tube lifetime owing to decreasing the temperature. Hence, by controlling the current of the Peltier thermoelectric coolers, the temperature of the laser was adjusted at 23 °C. In this case, however, due to the variation of the laser tube temperature around the temperature 23 °C, the length of the laser tube may alter, which in turn causes the movement of longitudinal modes on the gain profile of the laser and, consequently, an instability in the laser frequency. It is worth mentioning that before applying the stabilizing circuit to stabilize the frequency, the method of measuring the stability should be specified.

Fig. 9
figure 9

The laser output power versus the tube temperature: green dots experimental data points; blue line the best-fitting curve of the experimental data

In order to measure the limit of stability, one can utilize the difference of two principal axes’ intensities. Assume that I x and I y are the light intensities transmitted from the alignments of two principal axes indicated in Fig. 2. The temperature change results in the displacement of frequency modes on the line shape and, consequently, the variation of \(\Delta I = I_{y} - I_{x}\). The zero points of ΔI correspond to the state in which the frequency of longitudinal modes stay on the same distance from the central frequency on the line shape (Fig. 10a).

Fig. 10
figure 10

Signals related to: a light intensities transmitted from the alignments of two principal axes, I x and I y ; b the difference of intensities ΔI = I y  − I x

The maxima and minima of ΔI occur when one of the two modes is at the central frequency. Therefore, the change of ΔI by 2ΔI Max corresponds to the change of frequency of each longitudinal mode by the axial mode spacing (δν = c/2L). Thus, one can write:

$$\frac{{{\text{d}}(\Delta I)}}{{{\text{d}}\nu }} = \frac{{2\Delta I_{\text{Max}} }}{\delta \nu }.$$
(1)

This means that the stability (dν/ν osc. ) can be calculated by the following equation,

$$\frac{{{\text{d}}\nu }}{{\nu_{{{\text{osc}} .}} }} = \left( {\frac{{{\text{d}}(\Delta I)}}{{2\Delta I_{\text{Max}} }}} \right)\frac{\delta \nu }{{\nu_{{{\text{osc}} .}} }}.$$
(2)

By fixing the temperature at 23 °C and consequently the length of resonance cavity, it is expected that the frequency of the laser is stabilized on the gain profile; but the measurement of the laser modes via the method described in Fig. 1 showed that the frequency of each mode gradually moves at a rate of 800 kHz/s on the gain lineshape, which is, according to Eq. (2), equivalent to short-term (1 min) stability of 4.30 × 10−8 (~70×). The displacement of laser oscillation modes on the line shape, by any reason, will be caused the change of ΔI. Therefore, to overcome this variation, the switch S (in Fig. 6) must be put at position B. Consequently, the feedback circuit including the integrator prevents the frequency variation by controlling the length of the resonance cavity toward compensating the changes. This process is carried out so that the laser frequency always stays constant on the gain profile. The measurement of stability using Eq. (2) indicates that the short- (less than 1 min) and long- (more than 1 h) term stabilities are equal to 1.17 × 10−9 (~2700×) and 2.57 × 10−9 (~1200×), respectively.

After having stabilized the laser frequency, the measurement through an SF–PI reflects that the laser operates in two longitudinal modes which are symmetrically spaced from the central frequency on the gain profile. This, of course, was expected, because in this case, as explained earlier, although ΔI = 0, the variation of ΔI is the maximum. On the other hand, since the input of the stabilizing circuit receives a signal corresponding to the variation of ΔI, this means that the maximum sensitivity for detecting the fluctuation of frequency is associated with ΔI = 0, leading to a maximum frequency stabilization. Therefore, no matter in what state the control of the system to be transferred to the stabilizing circuit, the best stabilization is established at about ΔI = 0.

Conclusion

In this paper, an active method for frequency stabilization of an internal-mirror red He–Ne laser was scrutinized. First of all, the number of laser longitudinal modes and the direction of the laser principal axes were determined using a polarizer and an SF–PI. Then, the laser light power versus the discharge current was measured, and it was proved that there was an optimal current (5.5 mA) for which the laser power was the maximum. In addition, the measurement of the laser output power versus the temperature of the laser tube indicated that there was also an optimal temperature (23 °C) in which the laser power was the maximum. Therefore, the current of the laser tube was set at 5.50 ± 0.01 mA by an adjustable current source. High-precision current source prevents any alteration or deviation from the optimal current due to power supply instability or city electricity’s fluctuation, which, at first-order approximation, leads to a short-term stability of about 4.30 × 10−8. Moreover, the laser system was isolated from the environment using two thermal and acoustic insulator shells. To appropriately control the temperature of the laser tube, two Peltier thermoelectric coolers were connected to the laser box through an aluminum block. By adjusting the current of the coolers, the laser tube was set at the optimal temperature. Then, to overcome any fluctuations in laser frequency, the laser tube’s temperature was controlled by a feedback mechanism whose input receives a signal related to the difference of laser longitudinal modes’ intensities. The measurement by the comparison method signified that the stability of laser frequency for less than 1 min (short-term stability) is 1.17 × 10−9, and for more than 1 h (long-term stability) is 2.57 × 10−9, corresponding to a coherence length of the order ~250 m.